DM&IR 130: Resurrecting an SD9

28 01 2012

One of my first Missabe locomotives was a Proto SD9, it was actually a pretty good deal. Bought it off someone changing prototypes and scales and it wasn’t operational so he through it in with a number of ore cars. The original problem ended up being stuck bearings on the worm gears which made it a good deal.

After a while I started having problems though and eventually I couldn’t even run it reliably on straight track, no matter what I did it just didn’t work and I ended up giving up and putting it in my doesn’t work box in a pile of parts. Since then I’ve learned a few tricks both tuning up other locomotives and fixing car problems.

While troubleshooting a problem with my wife’s car my mechanic, and father, used dielectric grease to improve electrical connectivity between contacts on a connector. Shortly after than I ended up fixing a problem with DM&IR 413 and unpowered frogs by, among other tweaks, using dielectric grease on the power pickups. Then one day while digging through my parts box fixing one of my son’s locos I came across the frame and decided to give it the dialectric treatment. Before long I had it running pretty well.

One of my reasons for giving up on it originally was because it is a bit out of my era, the Missabe sold it in July 1996 but the tunnel motors from the SP didn’t start arriving until December of that year. This is one of those situations where when I’m running it I’ll invoke the stretchable reality clause.

The Prototype

DM&IR 130, and EMD SD9, was built 1957 and was one of 74 SD9s owned by the Missabe, including #110 which was originally EMD Demonstrator 5591. It’s my understanding that 130 is still around but just sitting having ended up on the now bankrupt Modac Northern.





Short Missabe Consist Video

26 01 2012

I managed to shoot a very short video of my Missabe consist pulling a coal train last night, unfortunately the combination of the camera not cooperating and having to make sure the main was clear to keep moving it was very short.





Birthday Operating Session

26 01 2012

Last night some friends and I had an operating session that happened to fall on my birthday (and the layout owners was the 24th!)

I took along DM&IR 210, 216, & 413 as well as EMDX 9003. It was the Oakway’s first time out for an Ops session and it ran flawlessly. It ran both solo and with 210 which also ran well (but I need to turn up the sound, its too quiet on a large layout)

I also ran all three Missabe units as a consist pulling some large trains including a large coal train, I seem to have them well matched as they really weren’t fighting each other. Both 210 and 413 ran well but 216 was a little rough so it will need some tuning. It also had some problems derailing on tighter turns, I suspect this was due to the very short coupler shanks and being in the middle of a consist.





Going to have to get him his own train soon

16 01 2012





All Cinched Up!

16 01 2012

One of the last outstanding wiring items on my CR23 module was to get some cinch jones plugs. They actually arrived a couple days ago so with today off work I wired up the jones plugs.

I had been using the accessories bus plugs (trailer plugs) as temporary track bus plugs so i have to wire those back up and get a second UP5 and then the wiring is done!





Train time

15 01 2012

I got some time this after noon to work on some train projects, re-assembling DMIR 216 and even got to a long standing project to revive an older Bachman F9 for my son.

While I was working on that my oldest son played with his switcher and switching layout.





Replacement truck for DM&IR 216

13 01 2012

Today I got a replacement truck from Athearn (I sent in the bad one a week or two ago). Looks like it’s even back in time to be speed matched for the next Ops session.





2011 in review

31 12 2011

The WordPress.com stats helper monkeys prepared a 2011 annual report for this blog.

Here’s an excerpt:

A San Francisco cable car holds 60 people. This blog was viewed about 1,400 times in 2011. If it were a cable car, it would take about 23 trips to carry that many people.

Click here to see the complete report.





Digitrax Notching Profile

31 12 2011

This week I had been looking for notched sound profiles for digitrax sound decoders (my SD38-2 has digitrax sound). I knew it was possible to do notching but the supplied SD38 sound profile did not do it.

Eventually I stumbled on to some files in the digitraxsound yahoo group where I found notched projects for the EMD 567 non-turbo, 645 non-turbo, and 645 with turbo. The 645 NT was correct for my prototype so I downloaded it to my SD38 this afternoon and I have to say it is a very nice improvement over the factory SD38 sound. The 645 projects were by Alex Stroshane and I have to say thanks to him for the great profile!





Little Engineer!

28 12 2011

We went down to visit my parents this week while I had vacation time so we set up the Thomas track for the little ones. Jacob, my youngest, has really taken to trains (18 months old) and he really had fun controlling Thomas!








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